Thursday 20 March 2014

Off with the Head


Well the head came off easily enough, and the studs were easily removed. (although one of the long studs isn't a Sprint one and was fitted without the steel washer under the nut).

However, on inspection the gasket and head look ok





The oil is just where I have wiped round the bores, after cleaning the water out









Although I am a little surprised that there are no honing marks in the bores as it is supposed to have been stripped and had new rings fitted.

So why did it boil over .....

it had a new water pump fitted by the PO ...





If you look closely at the gear teeth they are absolutely buggered !!! so is the jackshaft gear.

So its engine out time, strip clean and rebuild.

The pump must have been one of the NOS ones with faulty case hardening that were floating about a few years ago.

Luckily I have bought a spare Sprint engine for £160 that has had headgasket failure after a rebuild so this should yeild a good jackshaft, oil pump and water pump (and the head stud) - its also got a new Kent DMS1 cam, and oversize pistons - although it is seized (water in the bores I suspect) - but still a bargain as it will save £100s of pounds in new parts.

However it will delay returning the Sprint to the road as I now have to embark on a proper engine rebuild

Sunday 16 March 2014

Just as I thought it was all sorted.

I spent Saturday morning "fettling" the little jobs left on the Sprint.

The refusal to rev above 4500 was probably the 3 thou points gap (ye,s I should have checked earlier, but the carbs were that bad I couldn't notice the rev limit problem) - that sorted it will easily red line.

Next replace the rear brake auto adjusters (also purchased at Stoneleigh)  - I finally have a nice firm brake pedal with little travel, so Hooray all ready for the CT Dinner at Milton Keynes.

So Anne and I set off, bags packed looking forward to the party and the fun and games, when just short of J15 on tthe M1 the headgasket fails in a big way, I did manage to get it off the Motorway and it was recovered by the AA, but this car seems determined to stop me enjoying it. Its only firing on 2 or 3 cylinders now, and I wonder what I will find when the head is removed.

I am off on business trtavels to Russia for 10 days, so the car is going to have to wait until my return which may now make it an unlikely contender for the HCR, but watch this space.

Saturday 8 March 2014

Fitting Stoneleigh Parts

I had a good time at Stoneleigh, and got some excellent parts for the Sprint.

First off is this NOS exhaust



It sounds like a Sprint now its fitted, and all those nasty booming noises from the body caused by the "sports exhaust" resonating have gone.

Then fitted the NOS Tandem Master brake cylinder (as rare as a rare thing!) that with the reinforcing bracket between the servo and inner wing have nearly fixed the brakes, at least they feel like they will stop the car now, although there is a little too much pedal travel still.



I need to replace the auto adjusters in the rear drums because they work some of the time but not all.

However replacing the cylinder, let me recentralise the PWDA valve, so I do not now have a handbrake warning lamp on all the time.

Then I had to helicoil the front seat mount - won't be the last stripped thread on this car I think!



Now onto the carbs, and an attempt to fix why its not running right

Spot the deliberate mistake










Yes thats right K&N filters for a smaller size carb, partially blocking the carb mouth AND the venturi tubes that cause the piston to rise.

Fantastic, about the quality of engineering that I have come to expect :(

I need the secondhand Sprint airbox that I have been promised.

Remove the carbs next - not simple, instead of ordinary nuts with locking washer, nylocs were fitted, removal of these was a pain as access to the retaining nuts is limited, so on with a spanner, move it 20 degrees then remove spanner and reverse the spanner so the jaws are at a different angle and reapply to nut for another 20 degree turn, repeat processs until nyloc is unscrewed down 12mm of thread, do this 8 times for all 8 bolts. I don't believe it, most places there are no lock washers or nylocks where required on this car, but the one place you don't want nylocs, you get them Grrrrrr

Anyway removed the pots and pistons and what do I find, the rear carb had the jet screwed right up, the front was permamently in a semi choke position - due in the end, to a bent choke arm to the jet on that carb, so it wouldn't seat fully home when the choke cable was released. No wonder it didn't run right.

All reassembled, revs to 5k plus now, and no missing at tickover, its not quite right yet, doesn't quite pull as it should, need to look at plugs and points and dwell angle.

Its begining to be a nice car, drives without rattle or untoward noises, just need to get the brakes to 100%, and sort out the slight reluctance for the engine to rev freely - I'll enjoy driving it soon !

Where am I?